i think i need to dig into the 01290200 cache error that has been coming up. i'm concerned that an issue with my DBA-ESDI card has caused it, but i'm not sure.
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i think i need to dig into the 01290200 cache error that has been coming up. i'm concerned that an issue with my DBA-ESDI card has caused it, but i'm not sure. 57 comments
see? no cache or memory chips. the larger devices are probably semicustom gate array parts that IBM was fond of using. doubt they contain any cache memory. @tubetime looks like the error is generated by an NMI that gets tripped when the cache is being set up. could be a number of causes but in general it is an issue with the internal CPU cache. could also be this test of the DMA controller which is also included in the same set of tests and triggers the same error code, for some reason. hmm, the error still comes up. so i just tried what i *should have tried* at the start -- the 700 series diagnostic disk. when the diagnostic detects the cache error, it asks if you have replaced the CPU card. i *lied to it* and said that I had, so when it asked if i wanted to keep the cache disabled, i said "N". aaaand that fixed it! we're now booting to DOS off my DBA-ESDI disk replacement. so here's what i think happened: this is all very good because i know the root cause and it's not something terrible like data bus contention, and it's thankfully not permanent damage. it boots windows 3.1 now. it was trying to run a weird hdd power saving mode command I hadn't implemented. it also complains about the swap file because the filesystem is read only still. so about that write issue: it's an off-by-two error somewhere. two bytes being a single 16-bit word, so it's really an off-by-one error. @tubetime of course it is. 🙂 Thinking it was an off by two error was off by one. 😂 figured it out and fixed it. i forget to set the "transfer request" flag to kick off DMA. in another routine, it sees that this flag is clear and assumes that a word has already been read using DMA, so it reads a crap value and then sets the transfer request flag again to start the next DMA transfer. that "crap value" pushes the valid data forward by one word. on to the next issues: randomly the ATN register mailbox flag gets set but the data in it is stale. also, the status interface register will randomly get read from by the host. I think these are two facets of the same problem: the mailbox flags sometimes respond when you access a register that they are not supposed to be monitoring! the mystery deepens. according to the logic analyzer, temp_atn_set never goes high. reg_atn_set (for crossing clock domains) is always 000. flag_atn is only set to 1 on this single line of code! and yet, somehow, it magically flips to a 1. looking at the generated logic, i see no explanation either. temp_atn_set (aka sd_cmd, my test point) never goes high. no glitches, no nothing. to set the flop, EN must be high and R must be low, and a clock edge must occur. there's a glitch! that's why I missed it before, it's only 2ns. this is the signal from the MCA bus clock domain, and it's getting picked up in my other clock domain's edge detector. and i believe this is the cause. this line right here. each signal, la_*, is an output from a flip flop latched by the micro channel bus cmd line. however, this line of code creates some combinational logic--there's a timing hazard here... the problem? the line (la_addr == REG_ATN) creates a bunch of gates that are slightly slower than the simple AND gates in the previous part of the line. so la_mca_op=1, ~la_s0_w_l=1, and (la_addr == REG_ATN) *is also a 1 for a very short time!!!* this is because the previous value of la_addr WAS a REG_ATN. what i need to do is take that entire wire and turn it into a latch (a reg) and clock it on cmd. so here's the solution: all the signals in the MCA bus domain go to a latch clocked in that domain (the first "always" block). then *without any combinational logic* the output of that latch goes *directly* to another latch (the second "always" block) located in the main clock domain. (i have another flip flop in main clock domain just for detecting the edge) next step is to optimize the interface speed. right now it takes 25us to read a sector from the SD card but ~5 milliseconds (ouch) to DMA it to the PC! it's mostly an issue with the Teensy-to-FPGA interface, which is async and simple: 4 address lines, 16 data lines, a read control line, and a write control line. everything else is done as a register in the 4-bit address space. flag register for status and mailbox sync bits. why is it 5ms per sector for DMA? well, it's about 20us per word. most of that time is wasted by the slow interface between the Teensy and the FPGA. I really should fix that. got rid of some delays and now we're down to 6us per word. but there are some unexpected wide gaps in between transfers between the FPGA and the Teensy. ahh that must be the issue, when i change from a read to a write, i have to set the port direction for 16 IO pins. pinMode is uhh not quick, so let's try writing to the port direction register directly. so how does this compare with the real drive? it transfers a word in about 1.6us (compared to 2us for mine), so it is slightly faster for sustained data transfer with data that fits in the internal buffer. however, seek times (in the ms range) more or less cancel this out. here's a DMA cycle for the real hard drive. it's using the bus more efficiently, requesting a new transfer as soon as the transfer completes. my design waits for the full DMA cycle to end before requesting a new one. maybe theoretical maximum transfer rates would make the comparison easier: if i put in a bunch of work and implemented burst mode DMA transfer, i might be able to hit 4.5MB/s. no more debugging wires. the DBA-ESDI drive is now running stand-alone! I printed an angled carrier. the angle is because the socketed Teensy is really tall. time to lay out a version of this board for other PS/2 models, like the 50Z. this is the somewhat less uncommon 72-pin DBA-ESDI form factor. @tubetime Nice! (And LOLing because I JUST asked a client whether they really need the big teensy or could they go with the smaller one.) @tubetime Reading the silk screen of your boards is always so much fun! 😂 looks like there's a rare problem when reading sectors, around 1 in 100,000 reads. ugh these can be hard to track down i thought it might be a timing issue caused by disabling USB debugging, but it still happens (with roughly the same statistics) with USB debugging turned on. looks like some individual data bits are getting flipped. what's really odd is that it is repeatable and it seems to be the same bits at the same addresses. also -- there seem to be two overlapping bugs. one causes a few bits to be corrupted for single sector reads, the other causes an entire sector's data to be shifted by several bytes. huh, once I connect the logic analyzer, the problem takes much longer to reproduce; the probability of data corruption drops dramatically. interesting but it makes things much harder to debug. @tubetime hey @azonenberg weren’t you looking for examples of probes changing behavior of the DUT? looks like it is skipping a transfer here somehow. it transfers B66D, then it skips 6DDB and goes to DBB6. the preempt line seems to deassert right before arb/gnt goes high. that doesn't seem right. @tubetime Ugh, that's NEVER good. I see lots of oscilloscope probing in your future. @tubetime Why is there a SD Card slot forseen on the baseboard as well? @1000millimeter in case i want to use a soft CPU core in the FPGA instead of a separate Teensy @tubetime This was really enjoyable to follow along with! Congrats on the progress |
looks like the cache is inside the CPU. i can't find any cache chips on the motherboard.